Update Been a while since ive updated my thread in the last couple of months as ive been kept busy as some of you know i got a dodgy engine rebuild done in the first place which ended up been a full rebuild the second time around My block and crank were fuked which was the reason why i had problems in my recents threads, thrust washers were found in my sump when i was cleaning it out, the play that was in the crank was unreal The full rebuild was done with only genuine parts and the head and block done by martin tracy at westward engineering While the car was off the road done alot of sorting out. while the engine was out i cleaned the engine bay. Got the centre section cut out of exhaust and replaced for straight pipe which sounds way better now. Picked up an apexi boost gauge cause didnt like my racetech gauge in PSI. Order deep dish steering wheel for christmas. I also Picked up genuine livesport rear lip just has to be collected . Had a leaking coilover which i got rebuilt. Sold the JAM ECU and went for JAM FCD and Sard fuel pressure regulator. Its now ran in and just have to get fueling sorted by Martin Sum Pics to follow work done Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Click to see fullsize Enlarge this image Click to see fullsize Enlarge this image Click to see fullsize Enlarge this image Click to see fullsize Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Click to see fullsize Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image Enlarge this image