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white-gt

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Posts posted by white-gt

  1. no i agree mate start cheap.


    but why would the leak down test show a leak that we could hear in cyl 4 and feel it comming thru another cylinder and we then turn the crank and it doesnt do it again



    just been quoted £480 inc vat for all new pistons full gasgket kit and rings..


  2. ok i kinda understand.. but the smoke coming out is bluish so does that not mean burning oil ? i dont see how it can have too much crank case pressure just because one isnt going to the inlet manifold though, all that does is take in air so what difference would having a pipe from the over to the inlet do?


  3. ok i see what your saying but surely a fault would have shown before say 300 miles have been covered since i change the setup.



    its just a metal catch can with 2 inlets or oulets both the same basically and a breather on the top,



    so your saying one pipe from the cover to the catch can and the other outlet on the cover should be going to the inlet manifold the way it was before?

  4. i done a compression test twice now from 2 different places and they said it was spot on at 150 psi across all 4, so how is that possible if on a leak down test it showed a leak..


    the breather is oily and dirty but i dont suppose that would effect the colour of the smoke as its clearly coming out


  5. my rocker cover has both pipes going to the catch can and the inlet manifold pipe is blocked off this was only done in the last month, before i only had a breather on the left and a pipe going from the cover to the inlet mani.


    i changed the oil and filter about 2 months ago using shell stuff i usually use, recently had the fuel filter changed and fueling checked but it was running lean before i done that as the fuel pump was dying and i didnt know, it was only when it was on the dyno we seen it was up at 15 afr around 4k rpm, so fuelling is now spot on..


  6. ok so ive been having some running issues with it feeling more flat than normal, took it to a local dyno garage and got it inspected.;



    while doing a leak down test cyl 4 was passing some air but all the rest are tight, we rotated the engine and it held pressure solid after that..



    so on the dyno not pushing hard, revs held at 2500rpm and raising boost pressure we start to see blue smoke comming from the catch can but no noticeable smoke from the exhaust.


    im told its either piston rings or head gasket but needs opened up to find out for sure.



    so, is the smoke diagnostic correct?


    and if so, without talking about a large forged bill whats my best options ? standard toyota parts ? im not looking at going past say 230bhp on my hybrid setup.



    im sure he said he will rebore the cylinder or something also..



    any thoughts ? thanks


  7. hks actuator seems fine, found a tear in a boost pipe, replaced it, boost is faster spooling but still feels flat as shit.



    so if its not the boost controller or actuator because boost is reaching 1Bar, and its not the air filter as its new, and its not a leak, with no faults showing on the diagnostics wtf is it?



    does any one know if their was a fault would it still show even though the dastek unit is fitted? not sure where else to go with it


  8. ok so done a dignostics and nothing came back as faulty..


    changed the airfilter and still no better, checked the turbo and the blades look fine, their is some side to side but minimal in and out and still no smoke etc..


    if im driving in 2nd and the rpm is about 1.5lk and i floor it im not on full boost until just after 3k rpm and it doesnt feel like it picks up propper until around 4k rpm.


    the garage done a compression check, leak test and smoke test with no results..



    disconnected the battery for half hour also with no results.



    any other thoughts? im still leaning towards either the mbc or fueling again..


  9. ok so i put it into the garage to get it checked and they said they cant find anything wrong with it at all.


    compression is fine, leak test came back with nothing, cmoke test came back with nothing.



    he said it feels like its struggling in higher gears.


    so ive booked it into a local dyno to get the fueling checked again make sure its not over fuelling or under..



    any other thoughts? could the turbo be fucked even though its going to 1 Bar and no smoke etc?


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