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Kieran Barber

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Posts posted by Kieran Barber

  1. when I get a chance I'll try to snap a few pics, but i've found them to be imprecisely made, as in the passenger one fits perfectly but the driver's side is just short, and we had to make a few modifications so they would actually sit in the frame.

  2. Update time with good news, the misfire has been solved, looked like a lead was shorting onto the plug itself.

    This was on cylinder 1, i'm assuming that's why this plug has a scorch mark on it
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    And cylinder 4's lead was weak on top where it sits on the cam cover, noticeably harder to remove as it felt a lot weaker than the other leads.

    But got the new grade 7 plugs in and KV85 leads, looks a bit nicer now despite the cam cover long overdue a repaint.
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    another small thing to add is rear brake pads and rear passenger disc was replaced.

  3. The mk3 certainly grew on me overtime, I always liked the mk2 as my mum used to own the grey auto one bean now owns around 6-8 years ago and maybe further on, but I really like mk1 GT's as well.

    It's a shame that they're getting few and far between now, but it's how it has all gone mate.

  4. Update time, the NGK leads arrived along with my oil filter and spark plugs later last month, but the issue was that I noticed the lead diameter is too small, kind of like an oem+ sort of lead as they're only 5mm, but they'll end up on my mum's auto glanza so i'm okay with it.
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    Got a bit of a rust situation that has shown itself more recently too, but as winter comes, i'm hoping to restore her a little as the bodywork really isn't great and i'd like to get her under sealed.
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    As for other things too, I ended up buying some KV85 leads for maybe later down the line, and bought the mk3 grille off matt as his still had the badge intact, he also threw in one half of the boot trim that he had lying around, which i'm very thankful for.

    And as for that misfire, matt also suggested the rotor arm and distributor cap may have some small corrosion on the metal contacts, so I got some sandpaper on them and put it back together, but the problem still unfortunately persists.

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  5. Small update for the GT.

    So for a couple of months, it has had a small misfire whenever i booted it in second gear, first seemed okay and third onward seems to show no issues when boost came on.

    I ended up buying the NGK HT leads from nengun and some new Grade 7 Spark plugs from fensport to hopefully resolve the issue

  6. Hi there, just wondering if anyone on here has had any experience with NGK's run of HT leads, and if they're either as good or better than magnecor's lineup of leads.

    They will be going on a TD04 setup at 1.1 bar if this changes anything.

  7. The work has been done to her and she's running beautifully again.

    only headache I had after was for some reason, the guy working on it tried moving the pipe that went from the expansion tank to the rad so the writing was facing the correct way on the expansion bottle top.
    ended up kinking it and then rested on the power steering pulley, slicing it.

    so I had to cut that bit out and put a small metal fitting in the centre for now, will get another pipe soon though.

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