This took place yesterday... ...or tried to, got it on the dyno at TDi and mapping was done by Matt from AFR Tuning, got the throttle body changed up for an auto one with TPS, running 460cc injectors too and all the wiring and loom has been fitted and vacuum piping run for the HKS F-Con V Pro, yet as usual a problem arises...when running it they found the K24 had no nipple for vacuum on the tubby, so have had to order in some bits to fit a nipple on the inlet mani pipe before the tb. This meant my wastegate was not working after 0.8bar - nonetheless, it was mapped but only made 140bhp at the wheels, with a lovely diagonal curve, it boosts beautifully now and I barely have to move my foot which makes it seem so much faster, they reckon at 1.2-1.3 bar the 220-250bhp I'm after is easily obtainable - sadly it will have to wait til after JAE. Have also cleaned up the engine bay with some nice blue tubing and awesomely fitted the HKS ecu into the air box with all the pipe work running through the two air con holes, behind the dash so its all tidy under there and lovely, so Matt can just undo the old ecu and have access to the Fcon without the faff of pulling the dash apart again