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Car don't start helllpppp yesterday


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Driving my glanza manual fine since I owned it no ploblemz

Now It don't start drive it to my garge to get fuel payed went to drive and turned the key nothing not even tick over nothing

Had a look and as all alright tryed bump nuffin still doesn't even sound normal tick over like it trying to start

Took a close look today and it no turns over but dosnt sound normal just hi sound wining

Cheaked all wires leads there's a switch under the dizzy cap witch wires aren't connected ???? Wires have snapped or come away

Cheak fuel I got fuel and changed spark plugs got spark carnt hear my fuel pump I have a wilbrow 255 so should hear but no

Lights come on the dash bust just as you turn over all it dose is hi wining ??????

Helppppp

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Unsure on what it's doing never seen this before

Do I know what switch is under the dizzy ??

And I tryed jump start bump start differnt battery just nuffin

Turn the key all it dose it a hi whining sound belts are turning but nuffin else :/

Any one

Unsure on what it's doing never seen this before

Do I know what switch is under the dizzy ??

And I tryed jump start bump start differnt battery just nuffin

Turn the key all it dose it a hi whining sound belts are turning but nuffin else :/

Any one

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Just a high whining? Do you no if its getting fuel?

Pump might be shagged.

Could always undo the hose off your fuel rail and see if it fires petrol everywhere when you turn it over lol

Is the car actually turning over? You say the belts are spinning but are they engaging the cams etc?

Take the oil cap off and see if they are spinning.

Weird solutions but weirder has happened!

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Cheers for all the replies found out I got 17 teeth missin on my cam belt sliped went out of time and hit all the valves so there's no compression to start the car

So might be a new valve an seats job and head gasket or

Out of time and head gasket kit anyway

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100% mate, but it will depend on if the head has been skimmed before and how much has been skimmed. If you've lost compresson on a cylinder either you've dropped a valve head or some piston damage has occured, although tbh mate, if you've slipped that amount of teeth, you will lose compression because the valve opening and closing times will be all over the place in regards to TDC.



Bang a new cambelt kit on there dude and set the ignition timing, she should fire up :thumbsup:


Edited by AdamB
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So u recon to do a compression test on it first if reads fine bang a can belt and re time it ??

Or if the compression test reads 10 -15 say the u recon piston or valves damage ??

Also I dout it been scimmed before as it looks like original can belt lol ??

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So u recon to do a compression test on it first if reads fine bang a can belt and re time it ??

Or if the compression test reads 10 -15 say the u recon piston or valves damage ??

Also I dout it been scimmed before as it looks like original can belt lol ??

Compression test will be out if the timing is out as the valves will be all over the place
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You will need to fit a new belt first mate as if its skipped that amount of teeth you'll probably find the intake and exhsust valves will be open giving no compression.

Whack a belt on there and then do a comp test, if that comes back all good just fire her up :)

Dont go removing bits just yet, it will likely be something small.

Edited by AdamB
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Alright people just had a camera down the spark plugs to see I there any damage to the pistons or valves turns out there was NO DAMAGE

Yayyyyyy

So just a.case of new cam belt kit on

NEED THE TIMING INFO IF ANYONE CAN HELP ???????

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  • 3 weeks later...

Sorry people for the late reply

In the end I had no compression in 4 and the rest of them were on 50 or under I didn't blow the head gasket but snapped 6 valve springs so no pressure

I sent the head of for a full rebuilt and new set of proformance valve springs shims etc

Plus full gasket kit everything included new thermostat head bolts cambelt oil filter etc

Put back together it's alive

It was out of time and got loads of compression and runs amazing

Done my 500 + mile now

Dyno + wideband

Ran 217.8bhp

203.1 torq

Fueling spot on

Things looking up :D cheers for all the advice Tec etc :D

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