Overdue update.... Lots has happend and lots of changes.
So a short period after fitting the new turbo kit, Unfortunately my headgasket went and i was burning loads of coolant, I had Funny onion off the forum help me disassemble the head and strip to the block it look like it failed on cylinder 3 as bore was washed. overall everything else looked good, over the coming days i send the head off for a full rebuild new valve stem seals, valves re-seating, carbon removed and a skim. The head was very very slightly warped and 8 thou was removed. While the head was away i decided it would be a good idea to spray the engine bay and clean it all up as was not a huge fan of the silver. Once head was back we put it all back on no issues and car was back on the road again.
I thought my old oil catch can was letting the engine bay down a bit so i sent my rocker cover to RWDevelopments for AN10 fittings and a new catch tank. Also put a Civic rad in too as the old was was corroded and looking a bit crap, once everything was back together it looked like this.