ollie ryan
Member-
Posts
2917 -
Joined
-
Last visited
Content Type
Profiles
Forums
Wiki
Media Demo
Events
Everything posted by ollie ryan
-
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
yeah before i drove it i let it warm up -
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
so this weekends progress well on friday i recieved my new rad hoses and samco pipe to come off the turbo think its tidied up the bay abit then cut the intercooler piping to custom fit the K24 turbo then fitted the radioator filled it up and started the car up which i shouldnt of done! i didnt no you had to prime the turbo up before hand i went for a 2minute drive and its was pouring out blue smoke after the drive, i then primed it and took it for a 30second drive and it seemed fine but after letting it idle for 5mins its starting smoking again so possibly knackered the oil seals i also have a massive bost leak and the car is only running about 0.1bar so havnt even felt k24 power and it already looks like the turbo will have to come off im gutted! im going to take all the intercooler piping off, see if there is any oil in there and re-clamp it all to see if i can get rid of the boost leakand then go from there here is how i left it at the moment ready to strip down again next weekend if anyone has any suggestions on why its smoking other then seals please let me no so this weekends progress well on friday i recieved my new rad hoses and samco pipe to come off the turbo think its tidied up the bay abit then cut the intercooler piping to custom fit the K24 turbo then fitted the radioator filled it up and started the car up which i shouldnt of done! i didnt no you had to prime the turbo up before hand i went for a 2minute drive and its was pouring out blue smoke after the drive, i then primed it and took it for a 30second drive and it seemed fine but after letting it idle for 5mins its starting smoking again so possibly knackered the oil seals i also have a massive bost leak and the car is only running about 0.1bar so havnt even felt k24 power and it already looks like the turbo will have to come off im gutted! im going to take all the intercooler piping off, see if there is any oil in there and re-clamp it all to see if i can get rid of the boost leakand then go from there here is how i left it at the moment ready to strip down again next weekend if anyone has any suggestions on why its smoking other then seals please let me no so this weekends progress well on friday i recieved my new rad hoses and samco pipe to come off the turbo think its tidied up the bay abit then cut the intercooler piping to custom fit the K24 turbo then fitted the radioator filled it up and started the car up which i shouldnt of done! i didnt no you had to prime the turbo up before hand i went for a 2minute drive and its was pouring out blue smoke after the drive, i then primed it and took it for a 30second drive and it seemed fine but after letting it idle for 5mins its starting smoking again so possibly knackered the oil seals i also have a massive bost leak and the car is only running about 0.1bar so havnt even felt k24 power and it already looks like the turbo will have to come off im gutted! im going to take all the intercooler piping off, see if there is any oil in there and re-clamp it all to see if i can get rid of the boost leakand then go from there here is how i left it at the moment ready to strip down again next weekend if anyone has any suggestions on why its smoking other then seals please let me no -
how do i fit a tial external gate?
ollie ryan replied to ollie ryan's topic in Intake, Turbo & Exhaust
yeah i just want to run off the spring tho as i have no boost control -
how do i fit a tial external gate?
ollie ryan replied to ollie ryan's topic in Intake, Turbo & Exhaust
okay mate, at the moment i have no vac lines on or off the turbo or wastegate -
got a my turbo setup on and gone for drive and i have no boost at all, im not runnning any form of boost controller and running straight off the spring, do i need any vac lines coming off the wastegate?
-
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
just went for the first drive and it is pouring out blue smoke and the turbo isnt spooling how do you setup a external wastegate and im not running any form of boost control? -
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
i bought the polybush enigne mounts of steve gt mate so dont have a patrt nnumber im afraid -
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
will do a full update in abit got one or two little snags beforea video comes up -
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
she is alive and sounds so so savage! -
agree with tj dont sell! this is a minter and silly quick!
-
true legend!
-
amazing mate! love it and the underneath is so clean!
-
still got the loom?
-
hi mate can you pm me also what i need to fit the breaks, cheers
-
poopie
-
i have mesiters and find them comfy to be honest
-
desperate is a better word i think lol
-
sekk your door cards for extra money lol
-
romours going round they are going to kick of in kingstone and twickenham, so getting a tad close to me and all my cousins live round that area
-
croydon is having it bad now and birmigham is getting it! the pictures on bbc news at the moment are shocking!
-
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
right so todays update, K24 is still not complete, not alot left tho, all i need is some new nuts and bolts and to cut th intercooler piping which is simple enough here are some pics of the work how it looked at the start bumper removed for ease then to remove the old hybrid from this to this now thats out the way time to fit the new one old setup v new setup then i hit a few little problems, the old turbo kit used a different size nut and bolt for the downpipe and i need some new bolts for the bracing i put everyhitng back on to see how it looked once finished so here is an idea and finally the mess of the garage afterwards i wanted to heat wrap it but the manifold is so sexy i couldnt hide it it will all be finished next weekend,i was booked in to have my new midsection made up but will put that off a week to finish this big thanks to T J Wilson who popped over today and lent a hand and also i recieved some polybush engine mounts of steve GT on friday so will fit them soon all comments welcome as usual -
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
oil feed return pipe doesnt sit quite right so im going to have to rotate the turbo slightly but i cant get the down pipe off which means i cant get the mani off and now this all means i cant heatwrap any of it -
Ollie's 98 blitz powered K24 Cruise kitted Glanza
ollie ryan replied to ollie ryan's topic in EP91 Glanza Progress Blogs
lol cheers mate! im now stuck!
